It had apparently been everywhere twice and it still
bucked and snorted when she dug in her spurs on takeoff.
A Vacation From Teaching and A Week in the Service Bay
I had two
weeks of summer break right in the middle of the summer semester and I decided
to spend a week back at the Ford dealer.I’ve been teaching Automotive Mechanics and I’m constantly working on ways to remain
current in the field.
I put a few
tools together in a toolbox that was more portable than my rollaway and clocked
in first thing Monday morning.I wanted
to help out without stealing labor hours from the two regular driveability
guys, so I started out slowly and worked as a consultant and advisor, helping
out where I could.By the third day I
was there, the service advisors were throwing tickets at me like I was a
regular, but there was plenty of work for all of us, so the other guys didn’t
mind.I saw some interesting stuff I
could really sink my teeth into.
One example was a 1989 Crown
Victoria that popped and skipped in a really nasty fashion when the engine was
warm.Plugging the Service Bay
Diagnostic System between the TFI module and harness mysteriously repaired the
skip (it happens sometimes, why I don’t know), so I couldn’t use the SBDS Power
Balance or Spark Duration screens to determine the cause of the problem.If I had connected the ignition oscilloscope
right away, I would have found that the ignition coil polarity was reversed,
but as it was, I found out the hard way.The wires had become unlatched from the connector shell and whoever had
reinserted them had transposed the wires.I found the reversed polarity after an hour or so of doing one thing and
then another, but the coil had to be replaced before the Crown Vickie would run
right.
Buckin’ Bronco
Before I
tackled the Crown Victoria, I ran afoul of an interesting little Bronco II that
had a relatively simple writeup.
“Unit
skips while driving down the road” is a fairly common complaint, but this
was no ordinary problem.The little SUV
ran better than I expected on the test drive and it was smooth and responsive
on hard acceleration, but when it got warm enough to drop into closed loop fuel
control and started using Oxygen Sensor input to adjust the injector pulse, the
tailpipe started belching soot and I experienced the bucking and jumping the
owner wanted to correct.
Closed loop
fuel control is as old as oxygen sensors (which first appeared in the mid
seventies in Europe), and one of the interesting
things about a vehicle entering closed loop is that you should never feel it
happen. If you do feel it, something is wrong.And if you punch a Wide Open Throttle (WOT) and feel the system drop
into open loop, the engine will come to life again instead of running like a
slug.When you level out to a more
sensible throttle angle once more, the engine will generally run well for a
second or two until you feel it drop back into closed loop once more, then the
sluggish bucking will return.
Armed with a scan tool, a guy who
understands Electronic Fuel Injection can watch the PIDS and determine when
Closed Loop takes place. The problem was that Fords didn’t have datastream
capabilities in 1987, so I headed back to the shop to rendezvous with my old
friend, the Service Bay Diagnostic System.
SBDS
Mental Analysis
I was
thinking about my first course of action on my way back to the shop.I could check fuel pressure; older fuel
pressure regulators fail fairly regularly and cause the pressure to bounce up
near 100 psi, but when that happens, a WOT kick won’t clear the problem up.What I was feeling on my test drive was more
likely to be related to the relationship between the PCM and the Oxygen Sensor.
FORD VIP TEST CONNECTOR
Connecting
the SBDS to the VIP test connector, I ran a KOEO test (Key On Engine Off) and
pulled a code 41 from memory; there were no hard faults.Next I ran a KOER test (Key On Engine Running)
and got another code 41.This didn’t
necessarily mean the oxygen sensor was bad.There could be an Oxygen Sensor heater circuit problem, a shorted or
open signal wire, or, most interesting to me, a bad oxygen sensor ground.
Having a Look at the Graph
The SBDS
machine has a breakout harness that connects between the PCM and its connector,
and since I had entered the Bronco II at the beginning of my diagnostic
session, the machine knew which pin was what.Snap-on’snew DDC unit does
basically this same job on most vehicles from 1981 – 1999.I selected several pins and let the machine
build a graph, which is pictured in the first screen photo.The O2 Signal appears in yellow, with voltage
levels on the left and a timeline across the bottom in standard graph
style.Note the odd O2 voltage displayed
on the screen.Instead of nice humps
between zero and 1 volt, we have a negative voltage reading of–1.2volts raggedly making its way across the bottom of the graph.I had seen strange figures like this before
and they generally indicate a bad ground somewhere.The body-to-block ground can cause screwball
negative O2 readings which will clear up when the alternator is disabled, but
unplugging the alternator did nothing to correct this particular reading.I decided to check the O2 sensor ground.
First Graph
Well-Grounded Inspection
When the
2.9 Liter engine had been around for awhile, I began noticing a recurring
problem, particularly on Rangers and Bronco II units with automatic
transmissions.There is an orange ground
wire that leads from Powertrain Control Module (PCM) pin 49 to the back of the
passenger side cylinder head.It should
be clamped between the dipstick tube bracket and the head.The circuit inside the PCM depends very
heavily on this ground in order to properly read the Oxygen Sensor Signal, and
some technicians would forget to reconnect that ground when reinstalling the
transmission.Black smoke problems and
odd O2 sensor voltages were common with ground loose or disconnected.
Incidentally, the Ford 60-pin PCM
connector had five grounds leading to it until 1989.Pins 20,40, and 60 were connected to the
negative battery post or the vehicle body near the PCM.Pin 16 was a ground from the TFI module
mounting plate at the distributor, and finally, Pin 49 was the oxygen sensor
ground.In 1990, when the three-wire
Oxygen Sensor was supplanted by a four-wire sensor, PCM pin 49 fed a ground out
to the Oxygen Sensor from the signal return circuits inside PCM.Note: The ground on four-wire sensors was
going out to the sensor instead of coming in to the PCM from the back of the
cylinder head. Late eighties V8 engines with two O2 sensors actually had two O2
grounds, one to each head.Older oxygen
sensors had just one wire, with the ground provided at the point where the
sensor screws into the exhaust.
What I
found on my visual inspection of the Bronco II was an Oxygen Sensor ground wire
that had been connected to the wrong spot, which was a bolt on the upper intake
(see photo).There are simply too many
gasket and bolt points between this spot and the O2 sensor (which is in the
exhaust header pipe) for the PCM to get a good O2 sensor ground reading.Another ground wire is supposed to go under
that particular bolt, but that ground had apparently been attached somewhere
else.A lot of guys will put the orange
Oxygen sensor ground wire here to avoid fighting with the confined space at the
rear of the head, but it can be accessed fairly easily through the wheel well
(see photo), and I took the necessary measures to move the O2 Sensor ground to
the right spot.
Wrong Spot
Right Spot
Better Readings, but…
The SBDS
60-pin graph looked a lot different after I moved the ground, but there were
still problems.The nice switching humps
I had been looking for were there now, but the sensor was switching in the
wrong voltage range (see photo).
Second Graph
Notice the switch on the yellow O2
sensor trace was switching between –0.2 and +0.3.The PCM liked the signal a little better, but
the engine still ran ragged because the O2 voltage never broke into the rich
range above +0.5 volts.A quick look at
the oxygen sensor revealed a fairly new-looking sensor, so I decided to look
for further ground problems.
More Ground concerns
At the negative battery terminal, I saw a
nasty universal-style terminal of the type that I have no use for.Twenty minutes later I had replaced it with a
good solder-on terminal and the secondary grounds were securely soldered into
the terminal with the battery cable, but the SBDS graph kept looking worse and
worse.
Another KOER test produced yet
another lean code and I decided it was time to replace the oxygen sensor.I’ve seen sensors get out of sync with
what’s proper and pull that stunt.They’ll read within a range that would be acceptable if it were higher
on the scale, but the whole pattern of sensor operation will be out of line
with what the PCM wants and the engine runs accordingly.
Finally Fixed
The new O2 sensor made the little Bronco run like a
new horse.Pulling up a new 60-pin graph
cinched it.The range was proper and the
switching was normal.This is the
pattern that a driveability guy likes to see.
Third Graph
My final test drive went very
smoothly. The Bronco II performed like a Mustang compared to the old nag
feeling it had given me when I first drove it and it gave me some satisfaction
to know that I had managed to surgically make the repair without changing
several hundred dollars worth of hardware.