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In
the Clutch of an Explorer
By
Richard McCuistian
Sometimes the
simplest problems can be compounded by a lack of cash. Confusing circumstances
don’t help either!
1997 Ford Explorer
89,058 miles
4.0L Pushrod Engine
Manual
Trans
Clutch is difficult to operate; sometimes doesn’t release properly.
Horse Trading
The car was
a 1965 Ford “Custom” a cheaper model of Ford’s Galaxie for that year. The
fellow who owned it stopped by my dad’s VW shop one day said it used too much
gas and he wanted to trade for a smaller car.
My dad had a ragged old VW bug for sale, and the fellow was so eager to
get out of the Galaxie and into a gas miser that he offered my dad an even
trade. After the choke was adjusted on
the Ford, the 289 (equipped with a column shift three speed, no air or power
steering) actually got twenty-two miles to the gallon. It was one of my first cars (as the oldest
son of a shop owner, I had several) and I could drive it to the beach and back
on an eighth of a tank of gas.
Those of us
who pull wrenches for a living can be notorious horse-traders and when
prompted, we can regale for hours those who will are interested (and those who
aren’t) with story after story of engines, vehicles, and other such items we
acquired for next to nothing and nursed back to health with wrench smarts, TLC
and a few used parts we had in the shed or out behind the barn. Behind every such trade lies a story that
isn’t finished until the item in question passes from our hands. As for the ’65 Ford, I probably remember it
as a better car than it actually was, but sometimes I wish I had kept it.
Yet with
all the stories we tell about our own good fortune, each of us knows those happy-go-lucky
money-squeezing situations simply can’t and won’t work consistently in the
day-to-day grind of fixing broken cars.
Digging an old part out of a pile of junk to get our own toys running is
one thing; repairing cars for the public is something else entirely. It’s
impossible to consistently produce the endless supply of cheap used parts it
would take to get customers’ cars running on a shoestring budget. And while salvaged powertrain components are
widely used in our industry, most of us have lost dozens of labor hours as a
result of installing a salvage yard part that we relabeled a “junkyard part”
when we went to the trouble to install it only to find that somebody else had
already used the good out of it.
Needles and Linings
Most of my auto
mechanics students are on an extremely tight budget, and it’s not uncommon for
one of them to have a ticket written on their own vehicle. This month’s MA Garage story was born when
Steve (one of my students) decided to replace the slave cylinder in his 1997
Explorer.
This Explorer’s problem was that
the clutch pedal required some heavy thigh power, and occasionally the
transmission would clash while shifting into gear, particularly reverse. I encouraged Steve to go deeper than the
slave cylinder/throwout bearing assembly once he and his partner got the
transmission out; the difficulty in shifting and the gear clash he was
experiencing in reverse evidenced the fact that something was applying
rotational force to the transmission input shaft when the clutch was depressed
in spite of the fact that the clutch had full travel and no free play. It started out to be a pretty straightforward
job. Push, pull click, click, and drive
it home.
With the transmission out and the pressure
plate removed we found a clutch disc whose useful life had slipped away; the
lining was worn almost to the rivets. The
root of the undesirable input shaft rotation seemed to be tied to a
disintegrating pilot bearing.
Aftermarket clutches come only in
sets nowadays, at least in this part of the country, and the price of a matched
set hovers near $200, a little rich for Steve’s wallet. Fortunately, we were able to purchase a
clutch disc separately from the Ford dealer.
With the new slave cylinder cashing in at $55, the pilot bearing at $16,
and the clutch disc at $60, Steve had a bit more than $125 invested, but not
nearly as much as he would have with a parts house set.
I was fortunate enough to find an
old Ford input shaft from a trainer transmission, and Steve used it as an
alignment tool. In an hour or so, the transmission was back in place with a
minimal amount of trouble. Bleeding the
new slave cylinder is a pretty involved process in the Ford shop manual, but it
turned out to be a snap this time around.
The air burped out, the clutch pedal was nice and tight, and it didn’t
require nearly as much of a meaty leg to operate the pedal.
But with the engine started, it
became obvious that something was still rotating the input shaft, and the
problem was slightly worse than before. As a matter of fact, the engine had to
be shut off to get the transmission in reverse.
Steve decided to drive the Explorer for a few days until we could get it
back on the rack and re-yank the transmission for another look.
Another Look
The second trip Steve and Big
Country (his partner’s nickname) made into the bell housing revealed nothing
out of the ordinary on our initial inspection; the pilot bearing was still
intact and rotating freely, but I was interested in having a closer look at the
new slave cylinder. Steve removed it,
and we stood it up next to the old unit for comparison and found that the old
cylinder was about 3/8 inch taller. Our
line of reasoning was that the newer, shorter slave cylinder just didn’t have
the travel that the original cylinder did, thus it wasn’t completely
disengaging the clutch. It made for good
theory. To further undergird our hypothesis, we did some research and found
that the original slave cylinder was an earlier model; indeed, the stamping
number on the transmission was for a ’95 model; it was ostensibly two years
older than the Explorer we were working on (unless the F5TZ number was used in
the ’97 models), and Steve said he remembered the previous owner admitting that
he had replaced the transmission.
Steve and Big Country installed the
new slave cylinder, slid the transmission back in place, and found that the
hydraulic line wouldn’t mate properly with the second new slave cylinder’s
fitting. This clutch hydraulic line
snaps into the fitting using the same principle Ford fuel lines have employed
since 1991, but the fitting is substantially larger than a fuel line
hookup. For removal, a plastic sleeve
built onto the male fitting releases the fingers that hold the line into the
female part of the fitting, and shop manual procedures call for a special
forked tool to operate the plastic sleeve.
The line looked as if it should have snapped into the second new slave
cylinder, but it would pop right back out each time we tried to snap it in. How the previous installer had snapped the
line into the original slave cylinder is beyond understanding, and fluid
restriction due to the improper line hookup may have been the reason for the original
hard pedal concern, especially since we didn’t replace the pressure plate. From another transmission I was using for a
trainer, I retrieved another slave cylinder like the shorter one we had
rejected, and we could see right away that the fittings were indeed different. Steve pulled the transmission back, removed
the slave cylinder, and swapped the fittings to mate the line with the new cylinder.
Bleeding the Unbleedable
The first new slave cylinder had eagerly
embraced fluid and spit out air like it actually wanted to be bled. This second cylinder seemed to like air a lot
better than fluid. We couldn’t get it bled. The pedal stayed mushy and uncooperative. The Explorer stayed on the lift that weekend
and Big Country gave Steve a ride home.
Monday morning, with the
transmission removed once more, we found that Bi Country’s fitting swapping
operation had been hastily done and that the fluid had been leaking at the
point where the fitting feeds the slave cylinder. With the o-ring seal properly in place and
the transmission reinstalled, the slave cylinder bled out quite nicely, but the
clutch still wouldn’t release.
Confused by circumstances into
believing we had some sort of oddball mismatch between the ’95 model
transmission and the ’97 Explorer, we reasoned that the clutch had worked
properly with the longer slave cylinder in the first place, but that the clutch
disc had been thinner. We also reasoned
that the shorter slave cylinder had worked better with the new clutch disc than
the longer one did. With that in mind,
we decided to reinstall the shorter slave cylinder, but with a homemade steel shim
installed between it and the bearing cover that would give it the necessary
support, yet enable it to have more travel.
With the transmission back in place and the cylinder bled out, we had
the best pedal we had ever felt when that silly modification was made, but the
clutch still wouldn’t release, and the concern actually seemed to be getting
worse.
This was getting ridiculous;
replacing a clutch isn’t rocket science:
We were obviously missing something very basic.
One of the other students claimed
he had fixed a problem like the one we were having by replacing the pressure
plate. I wasn’t convinced. We took the clutch back out, removed the
flywheel, installed the clutch disc and pressure plate on it, and mounted the
whole assembly in the shop press with the dummy input shaft splined into the
clutch and inserted in the pilot bearing. Utilizing an old locked up slave
cylinder and a big socket, we depressed the diaphragm spring until we could
rotate the clutch disc. We marked the
amount of travel required to release the clutch. The fingers had to move a full ½ inch to
release the clutch.
I picked up a Ford authorized remanufactured
pressure plate from the dealer, and we performed the same press test, comparing
the travel required to release the clutch.
The new pressure plate actually required more slightly travel than the
old one. So much for the pressure plate
theory!
Finally!
Taking another really close look at
everything in the bell housing once more, I decided to slide the clutch disc on
the transmission input shaft and spin it.
At first it seemed to be straight and true, but then the more I observed
it from different angles, the more I realized the disc was slightly warped. Fetching a dial indicator, I set it up to
measure lateral runout and found a whopping 0.065 inch of runout that would scrub
against the pressure plate and flywheel, effectively rotating the input shaft
and sabotaging the release operation of an otherwise healthy clutch assembly.
Since a transmission jack was used
and we never forced it through the clutch disc splines with long bolts or let
the weight of it hang, we had to conclude that the remanufacturer had relined a
warped disc without checking it for lateral runout.
Conclusions
Steve and Big Country did a lot of
work on that Explorer, but there were a couple of “up” sides to the deal.
1.
Nobody who watched this drama unfold and understood
what was going on will EVER install a clutch and pressure plate without closely
examining the disc for lateral runout.
2.
Steve and Big Country can now remove and reinstall an
Explorer manual transmission in less than an hour; not bad for first semester
auto mechanics students.
3.
The fact that it was Steve’s personal vehicle made him
a lot more motivated than he ever would have been if it had been a trainer
unit.
All in all, it was an excellent experience none of us will
forget any time soon.
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