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Richard’s
Law of Accelerated Entropy
The first place the guy went after he bought his truck was
to his cell phone provider. At that point, Richard’s Law of Accelerated Entropy
took over.
Vehicle: 2000 Ranger
Powertrain: 2.5L I4
Mileage: 108
Symptom: No-start,
Power locks inoperative
Immediate Deterioration
Everybody
knows that if you park a brand-new car in the woods and leave it there it’ll
begin to deteriorate. If you go back two
years later, even if the engine will spin over, it probably won’t start. Two years later, the battery will certainly
be dead. It may have one or more flat
tires. This is an example of the Second
Law of Thermodynamics, or “The Law of
Increasing Entropy.”
This brings us to
what I call “Richard’s Law of Accelerated Entropy.” In trying to improve their cars, some owners
will immediately shave thousands of dollars off the trade-in value of the
vehicle. We’ve all seen it. Somebody
(usually a guy) will buy a brand-new car or pickup and take it to have the
exhaust ripped off from the catalysts back so they can have mufflers installed
that make it sound like uncle Burt’s ’57 Chevy.
Or they’ll have the factory radio yanked out of the dash and some
gung-ho audio system installer will make mincemeat of the wiring in the process
juicing up the guy’s sound system so he can rattle windows in any neighborhood
he’s driving through. What about the
folks that butcher the suspension to lower the belly of the ride and install
those tiny little tires that make the car ride like a jersey wagon and render
it impossible to drive the vehicle onto the front-end alignment lift?
In the case
of this 2000 Ranger, however, the modifications were meant to be minor. On the
surface, it looked as if the cell phone installer did an exemplary job of
mounting the phone, and he was no dummy.
He had put phones in Rangers before, and never had a problem. This time, however, when he tried to start
the truck and back it out of the shop he wound up having to call a tow truck.
No Fuel Pressure… Why?
When Ryan,
my helper, found the Ranger on the service lot, it was unstartable. The engine spun but wouldn’t fire. A moment later he found that it had spark,
but no fuel pressure. After a quick check of the fuses, he found a blown 20-amp
fuse in the Power Distribution Center (PDC) under the hood.
Replacing the fuse,
Ryan found that switching the key to “run” popped the fuse like a tiny
flashbulb. When I got out there, I didn’t hear the fuel pump hum when I turned
on the key. That was good, because it’s
better to have a dead short that’s dead all the time instead of a come-and-go
problem that drives us all batty and keeps coming back every few weeks.
Overview
The
Powertrain Control Module (PCM) on the Ranger energizes the primary side of the
fuel pump relay when the ignition is switched to “RUN”, closing the relay’s
secondary contacts and powering up the pump for only a couple of seconds unless
the engine is spinning.
The fact that it
blew the fuse after we switched the key on was a sure indication that the short
was between the fuel pump relay and the pump itself. Occasionally, the fuel pump itself can be
shorted, and this was a new truck, so it wasn’t beyond the realm of reason to
think the pump might be the source of the problem.
I had Ryan feel of the
relays while I switched the truck on, so we could see which relay was the fuel
pump relay. He claimed to have
discovered the relay that clicked on, then off when the key was switched on,
then unplugged it, and we checked by installing another fuse to see if the short
was still there. We found that nothing had changed. It blew the fuse
immediately.
I had Ryan to operate the
key and found that he had fingered the wrong relay. I popped the relay Ryan had pulled back in
place (I ultimately found out that I had put that relay in the wrong place, but
I’ll talk about that later) and pulled the fuel pump relay. The short was gone. We pushed the shiny new
truck into the service bay.
“Ryan,” I said, “go pull up a
schematic of the 2000 Ranger Engine Controls.”
Following the Map
A quick study of the schematic
showed that the blown fuse had been feeding the secondary side of the fuel pump
relay, which explained why it only popped when the key was switched on.
Connecting the test light alligator clip to the positive side of the battery, I
gently wedged the probe on the test light into the relay terminal
feeding the pump, so as not to distort the terminal, but so the light would
stand up and be easily visible. Even if there was no short, this should light
the test light bulb because of the continuity through the pump motor brushes to
ground.
I opened the passenger’s door and rapped the inertia switch with the
heel of my pocketknife. The button on the switch popped up and the test light
went out, so the short had to be between the inertia switch and the pump. The map showed us that our circuit went
through C309, a handy 40-pin connector Ford put in the floor pan on this
particular model. The connector was
quite easily accessible from underneath.
Resetting the inertia switch, I had Ryan roll under there on a creeper
and disconnect the big floor pan connector.
Our test light stayed on, indicating that the short was between the
inertia switch and the point of exit from the cab to the fuel tank, which was
connector C309.
Locating the Short
When I found the point where the
harness disappeared under the carpet, it lined up perfectly with the place
beside the console where the phone installer had drilled his holes (see
photo). It would have been wise to look
here first. Removing the console and
pulling the carpet back, I saw a nasty hole in the metal of the transmission
tunnel. That screw had missed the
harness, as had one other screw, but the third screw went straight through the
center of the harness and the sharp sheet metal threads managed to saw their
way into the wire leading to the fuel pump.
Very little actual damage was done
to the wire, but enough contact with body ground was made to overshoot what the
20-amp fuse could carry. Repairing the
wire and reinstalling the console, I remounted the phone holder in a more
innocuous fashion, this time avoiding wire harnesses with the screws.
Door Lock Problems
The service
writer had originally printed the repair order with the no-start complaint,
then added a handwritten addendum about the door locks being inoperative
also. When I tried the power locks, they
wouldn’t operate with the key fobs or the door panel buttons.
The door lock actuators in the
doors are operated by relays in a panel above the driver’s right foot. The common
terminal on each relay feeds the both wires on each actuator with a ground when
the relays are at rest. Energizing one
relay will switch the common terminal on that relay from ground to B+, which
runs the door lock actuator in one direction, while energizing the other relay
reverses the polarity to the motor, reversing the motor’s movement.
This is an old method of controlling DC
motors that has been around for a very long time in automotive applications.
According to the wiring schematic, fuse 3 in the battery junction box and fuse
20 in the fuse panel under the dash were both responsible for powering up pins
on the Remote Keyless Entry Module RKE or RAP, as Ford calls it), which was
located behind the passenger’s side kick panel.
Checking with my low impedance test light, I switched on the key and
found a good 12 volts at pins 12 and 20 on the RKE module.
Moving my test light alligator clip to B+, I
found that good ground signals were delivered to the proper relay coils (unlock
is pin 11, lock is pin 22 at the module) when the RKE fob was operated on lock
and unlock, but the lock and unlock relays weren’t responding. My schematic showed the positive side of each
relay coil was supposed to be “hot at all times”, but when I moved the test
light’s gator clip back to ground and checked at pins 11 and 22, I found no
power coming through the coils to the module.
(If the relays aren’t energized, the 12 volts feeding them should light
a high-impedance test light through the wire leading to control pins 11 and
22.
A low-impedance light will actually
close the relay’s primary windings like a short to ground.) The wire map for the RKE gave no indication
of where the “hot at all times” power was supposed to come from.
Moving from
the RKE wiring map to the Power Door Locks map, I found that instrument panel
fuse 18 was supposed to deliver power to the “Hot at all times” side of the
door lock relay coils.
“AHA!,” I said.
It only took a second or two to
move back to the instrument panel fuse block and find that fuse 18 was
mysteriously missing. I felt like a
dummy, having gone the long way around to find that somebody at the cell phone
place had apparently snatched a fuse.
Generally speaking (not always),
when something doesn’t work and you see and empty fuse position that has both
terminals, it’s smart to pop a fuse in there and see what happens. I got burned back in 1984 on an inoperative
cruise control this way. I installed the
proper size fuse in position 18 and the door locks came alive. I was kicking myself. I should have found
that problem quicker than I did, but now I was done. Or so I thought…
Another Job Well Done… Almost!
As I was parking the truck back on
the service lot, I found more problems.
When I punched the “lock” button on the fob twice to lock the doors and
chirp the horn, the park lights flashed but I heard no horn. I was beginning to get a little
irritated. Every time I thought I was
done with this heap, it would show me a new problem that demanded
attention.
I unlocked the truck again
and tried to blow the horn by pushing on the airbag (incidentally, this seems
like a dangerous arrangement to me; most folks are prone to get on the horn
button right before they crash…), but the horn was unresponsive. I had no
junction box diagram with me, but I remembered that relay swapping business
when Ryan and I first checked the truck, and I eyeballed the position of the
relays in the junction box under the hood.
My own Law of Accelerated Entropy was nipping at my heels.
There were some empty relay sockets
for optional equipment that was absent, so it had been easy to plug the relay
Ryan had removed back into the wrong spot.
I pulled the relay I thought I had installed in the wrong place when
Ryan misidentified the fuel pump relay, and plugged it into the horn relay
position.
The horn started working then,
but when I checked the rest of the stuff, the wipers had gone dead. This was really beginning to annoy me. It took
me about five minutes playing “musical relays” to figure out which sockets were
supposed to be vacant and which ones were supposed to have relays in them.
“Those cell phone guys have this
truck so fouled up nobody can fix it!” I muttered.
All’s Well that Ends Well
It was
humorous how that relay business humbled me as I was patting myself on the back
for finding the cell phone installer’s goof.
Those of us who have been pulling steel and chasing sparks for a while
can make some funny mistakes. I’d like
to hear your stories, if you have time to e-mail them.
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