After
an engine swap, a vehicle is supposed to run better, not worse!
1996 Mazda 626
2.0L Engine
CD4E Transaxle
122,653 miles
Unit
vibrates at idle; doesn’t run good on the highway.
Sick
Six-Two-Six
At
the risk of offending somebody out there, let’s begin by making the assertion
that any technician who is worth his salt will finish what he starts. I can remember a few technicians I’ve known
in my tenure who really enjoyed fixing cars… to a point. They liked the nuts and bolts aspect of
engine work but once all the fasteners were torqued and it came time to get the
engine running right, they’d “call for the calf rope,” so to speak, hoping
somebody would waltz by, turn a magic screw and put a hose in place to make the
car start and run right, effectively bailing them out. Isn’t it nice to be paid the flat rate hours
it pays to swap an engine and not have to worry about ironing out the kinks? As fuel, emissions, and ignition systems
become more complicated, it seems that more and more customers come to us and
begin their story with the words
“I had the engine
replaced, and…”
This
626 was a classic example. To begin
with, my phone conversation with Debra (the lady who owned the car) wasn’t as
detailed as it should have been. She and
her husband had paid a local shop about $1500 to install a salvage yard engine because
the original engine had developed a knock and after the job was done and the
bill was paid, the car didn’t run as well it had before the previous engine
started knocking.
Debra
described the problem as a “vibration” and I immediately began thinking of
driveline or wheel balance problems.
When we finally spoke face to face as she was filling out the paperwork,
it turned out that the vibration to which she was referring happening when the
car was sitting still. When the students
started the vehicle and showed me the idle problem, I had to admit that it was
pretty excessive, in spite of the fact that even a healthy 2.0 platform has a
tendency to send a mild jiggle through the steering wheel at idle. The MIL light was on (although I didn’t
remember her mentioning it), so before we did the highway test drive, I had Jimmie
plug the Hickock NGS into the DCL and have a quick look at what was stashed in the
memory.
Rich
Problem or Lean Problem?
The
P-codes we received showed that the fuel control system had reached maximum
compensation for both lean and rich conditions. While such a combination of codes sounds
peculiar, most of us have seen this little syndrome before. One possible cause of this concern is an
oxygen sensor that drops offline long enough during closed loop operation for
the PCM to ratchet the Short Fuel Trim ‘way up into the +20’s percent range and
stay there long enough for the Long Fuel Trim to follow its more sensitive
little brother to the rich side of the control band and file the lean code
while coating the ceramic zirconia O2 sensor bulb with a nice layer of
hydrocarbon soot. Then just as suddenly,
the O2 will decide to start telling the truth again, but now the Long Fuel Trim
numbers will have been corrupted enough by the dead sensor that the suddenly
truthful O2 sensor will instantly begin to reflect a rich-running engine, and
the problem remains persistent enough while the soot is burning off that both
Short and Long Fuel Trims will drift deep into the – 20 percentages, and now
the PCM has stashed the opposite code in its folder. Since this phenomenon can be terribly
intermittent, it’s not at all unusual to see normal datastream numbers at the
time of testing, along with a normally running engine.
But
the Mazda wasn’t running right at all.
The idle was far too rough, and a quick peek into the datastream
revealed numbers that were anything but proper.
The Fuel Trim Readings were dancing around the -25% mark, but everything
else looked fairly normal, with the exception of a MAF voltage that seemed a
bit too high. Ordinarily, MAF voltages
will run in the .7 to 1.0 volt area, but this MAF was reading nearly 1.2
volts. Checking the idle air bleed screw
on the throttle body, we discovered that it had been backed almost all the way
out; somebody was desperately trying to smooth the idle by giving the 2.O a
little more speed with a closed throttle.
After running the idle speed screw back to its normal position (650-750
rpm with the Air Control valve disconnected and the cooling fan not running),
neither of us was satisfied with the idle quality, (let alone the scan tool
readings; MAF still seemed a bit high) but we opted for a highway test drive.
Anemic
Acceleration
Chrysler
hung on to the Manifold Absolute Pressure sensor and stayed away from the
annoying MAF, so Chrysler/Dodge/Jeep techs haven’t had to worry with the
bucking and jerking that can be caused by a crack in the air inlet tube. How many times have those of us with
experience seen a buck-jerk or serious surge problem due to an unmetered air
leak that would shift fuel delivery to an intolerable range as soon as the
engine torqued back on its mounts? With
the engine rocking into and out of a hard pull due to power that came and went
with the opening and closing of an air tube crack, the situation can feed
itself to the point of bouncing your head off the headrest. The Mazda ran a lot like that, but the
problem only seemed to occur at about ¾ throttle. If Jimmie pushed his foot past the ¾ throttle
point, the car would hunker down like it was starving for fuel. Right at the ¾ throttle level, the 626 would
buck and jump, and below that, apart from the rough idle, the engine ran
normally, albeit a little weak on takeoff.
The TP voltage was sweeping smoothly all the way from .50 volts up to
about 4.60 at WOT, but the O2 would go lean, even though the PCM should have
been delivering full enrichment at that load and throttle angle.
“What
do you think, Jimmie?” As student and
instructor, we were about to enter opportunity for a rapid learning curve, and
Jimmie was eager to make the call.
“I
think we need to check the fuel pressure,” he postulated. It made sense. We headed back to the shop.
Fuel
A’plenty; Still No Power
Fuel pressure that drops in a hard
pull is a dead giveaway, and will usually show up on the gauge even under
no-load snap of the throttle in the service bay. With the fuel pressure gauge connected (it
takes a special adapter) and taped to the windshield, we test drove the car and
found a smooth 45 lbs of fuel pressure even the heaviest acceleration. With
that piece of data under our belts, it was time to look a little closer at the
scan tool readings.
With
an under-load stallout problem, it’s only natural to suspect fuel pressure or
quality.While the gauge might show
tattletale pressure loss on a heavy no-load service bay accelerator snap, the
smart way to check the pressure in a situation like this is to record the
numbers with the pedal to the metal in a hard pull. And unless this gauge was reading air or water
pressure (which, as it turned out, it wasn’t) this number looked good, even under load.
At wide open throttle acceleration,
as we peered through our window into the system, we reiterated the discovery
that both O2 sensors were reading lean, Short Fuel Trim was at 33% and that the
Mass Air Flow (MAF) sensor was reflecting only 2.78 volts.
When I teach my Power Stroke diesel
workshop, one of the principles I hammer on is something I learned twenty years
ago when fuel injection was still relatively new. We’ve all applied the principle, but
sometimes it helps to verbalize it.
A
technician who carefully studies and learns to recognize normal readings on a
particular vehicle or system can usually pick out an out-of-the-ordinary set of
signals and find the source of a concern in short order. Understanding the nuances of a particular
system and being able to compare one signal in a system to another signal that
should respond in a particular way is one of the defining qualities of a
technician’s knowledge base and becomes a powerful tool that enables the Top
Guns in this industry of ours to surgically repair vehicles that have whipped
other technicians for days. What we have
to learn to do is interpret the inputs and outputs in their correct
correlations the way the PCM does. There
are some correlations that are fairly standard.
This is what the MAF should look like at Wide Open Throttle (WOT).
For
example, if the PCM commands an IAC percentage increase on an idling engine,
the MAF doesn’t reflect increased airflow, and the rpm doesn’t increase, the
PCM has the idea that the IAC isn’t operating.
When a PCM knows there isn’t an electrical concern but can’t detect a
physical change with correlating sensors after commanding an input, a
“performance” code is set, and it will be defined that way on the scan tool
when the code is retrieved. We as
technicians can think the same way when we learn how.
In this case, while we had no MAF
code at all, it was becoming evident that the MAF wasn’t tracking with implied throttle
position the way it should. Any of us
who have seen scan tool graphs are aware of the fact that MAF and Manifold
Absolute Pressure (MAP) generally respond in direct correlation to Throttle
Position.
Also in this case, the MAF was
responding fairly normally up to 2.78 volts (see above - this MAF reading was taken at Wide Open Throttle), but was unable to rise beyond
that. And since the PCM was seeing the
MAF respond to TP changes, it stored no code.
It was a beautiful example of what service engineers call an “In-Range
Failure.” My student Jimmie, with his
limited experience and understanding of scan tool readings, had no clue that
the MAF wasn’t performing as expected. For my part, it took me longer to
recognize the problem than it should have. When we disconnected the MAF sensor,
the PCM defaulted to a strategy that operated based on its other inputs, and
the Mazda accelerated smoothly and powerfully.
MAF
Stuff
MAF anomalies can be extremely hard
to spot. In many cases, I’ve personally seen
an engine with an MIL light, rich or lean P-codes, and double digit fuel trim
readings (either positive or negative) and no other apparent problem, then discovered
that a known good MAF was reading just a few measly millivolts above or below
the existing part. For example, the
difference between 0.760 millivolts (which we’ll call the normal reading on our
hypothetical vehicle) and 0.830 millvolts (the actual reading on our hypothetical
vehicle) can cause the PCM to ratchet fuel trim figures deep into the -20
percentage band. Only a tiny difference
on a 5 volt scale, and not enough to cause a noticeable driveability concern, but
plenty enough to cause the PCM to store a code and illuminate the MIL.
Another important input provided by
the MAF is Barometric pressure, and on this type sensor, it reads in hertz,
like the old Ford MAP sensors. This
sensor likes to rest at about 153 hertz, and anything below or above that is
suspect. A MAF sensor can also respond
sluggishly to changes in airflow and the engine will run that way when it does.
On older GM cars, a white box
aftermarket MAF might give acceptable hertz readings, yet still toss an MIL if
the PCM doesn’t like the sensor for one reason or another.
What about those wonderful Asian vehicles? Well, their MAF sensors go bad too, and I had to replace a Japanese-made MAF a few
years back that destroyed a dozen of the customer’s Ben Franklin notes when the
bill was paid. (It was a $1200 part). A MAF sensor for an American car costs a small fraction of that. We were told at one class I went to a few years back that it would cost more money to buy all the fuel injection and emission replacment parts on a Mitsubishi vehicle than the full sticker price of that same vehicle when it was new.
Conclusion
On
our Mazda 626, the MAF range was a little high on the low end, and a little low
on the high end, causing the engine to run rough and rich at idle, then to run
lean and weak with the throttle and actual airflow above what the MAF was able
to indicate. This explained the rich and
lean P-codes in our case. There was no problem with the O2 sensor.
Debra gave us permission to replace
the $175 sensor, and I would have retained the old part except for a $75 core
charge. The 626 drove a whole lot better
when we were done.