While I’ve
done my share of automatic transmission work, I’ve really never been a big fan
of it. I even did transmissions as a specialty for awhile, but I never enjoyed
fibers, steels, snap rings and spool valves as much as the computers, wiring,
spark plugs and sensors of the driveability area. Admittedly, when electronics
invaded transmissions, they became a bit more interesting.
It’s not that the money is any
better in driveability/automotive electronics.
It takes a lot of grit to do what we do, and it takes a special kind of
a guy to enjoy doing automatic transmissions. A tranny guy worth his salt in a
busy shop can take some pretty astounding paychecks home at the end of the
week. But we all know that takes a tech
with the right stuff and even more true grit than Rooster Cogburn to hammer out
a living and enjoy doing transmissions day after day; you gotta love it or
leave it.
Back in the
mid eighties I when the A4LD was relatively new, I went through a spell when got
really tired of transmissions. The
valves in that incredibly complicated valve body were aluminum instead of
steel, (meaning you couldn’t get them out of their bores with a magnet) and
when some failure generated a mess of metal filings and scattered them among
the spools, it could take most of a day just to clean the valve body.
I rebuilt one of those units once and it left
the shop working just fine. It came back
about three weeks later still working fine as far as I could tell on the follow
up test drive, but the customer said he had dropped it in gear and it ‘didn’t
quite catch the way he thought it should’ one time a couple of days earlier. When somebody else is calling the shots and
giving the orders, it can be particularly frustrating. In spite of the fact that neither I nor the
shop foreman could duplicate the concern, the shop foreman insisted that I tear
the unit all the way back down and allow him to inspect all the parts. I yanked it out and tore it down, and when he
couldn’t find anything wrong in there, I was as angry and frustrated as I had
ever been up to that point in my life.
Deadbeat Dodge Dakota
The first
transmission I ever rebuilt was a 727 TorqueFlite, and as I was carefully
disassembling it and laying the parts out on the bench, a nosy older man who
had done some transmissions in his time came by, and true to form, he removed
one of the inner lip seals and inspected it while my back was turned. Since I hadn’t removed a seal from that slot,
I didn’t think to put a new seal back in there.
We all know it’s best to keep our hands off somebody else’s work,
particularly when so many parts and critical steps are involved.
This month’s vehicle was a high
mileage Dodge Dakota that came in on the hook because the transmission would
barely pull out of its tracks in forward gear; it responded a little better in
reverse, but it was still no prize winner.
This 42RH unit is basically a modified 904 Torqueflite (32RH) with an overdrive
compounder unit (outfitted with an additional planetary gear set) which
replaces the extension housing and provides a fourth gear ratio of 0.69 to 1 to boost the fuel economy at road
speeds.
I gave the Dakota
job to Josh and Red, two of my students, both who had practical mechanical
experience, but no real internal transmission experience to speak of beyond fluid
and filter changes.
The
transmission was full of dark, smelly fluid and a quick pressure test at idle showed
that it had enough line pressure to apply the clutches, but with the fluid in
the shape it was in, a pan snatch was the smartest next step.
The pan was
loaded with glitter and the dark fluid residue, and the magnet was nice and
fuzzy with metal whiskers.
From Truck to the Bench
A couple
hours later, Josh and Red had the transmission spread out across the bench in
all its glory, and there was nary a burned clutch or hard seal in sight. As a matter of fact, all the internal hard
parts (including the disassembled pump) looked just as pristine as the
clutches, with the exception that there were metal particles of various sizes
everywhere. It was one of those
confusing situations that left these burgeoning techs wondering what the heck
was going on and what they needed to replace in order to get this problem taken
care of. In other words, a ‘pizza box’
repair wasn’t going to straighten this one out. There was only one place left
to look.
Taking the
front clutch housing with its turbine shaft, I went to the torque converter and
found the problem. Engaging the turbine
shaft in its splines, I found that the turbine had welded itself to the
impeller. Among other things, a loose
transmission filter or damaged filter seal can pull air into the fluid supply
and cause a failure like this, because the resulting air bubbles always find
their way to the center of the converter when it’s spinning, and that’s the
part of the TC that needs lubrication the worst.
This filter
wasn’t loose, but it was evident that the Dakota would need a replacement
torque converter and while we were in there, we might as well replace the
gaskets and seals, and we should obviously take the time to clean the valve
body and the governor (the 42RE electronic version of this transmission doesn’t
have one). Since the fluid leaves the
torque converter in an unfiltered stream and goes to the transmission cooler in
the radiator, it was a foregone that the cooler would be loaded with metal as
well.
One of the
first jobs my students did when I started teaching back in 2001 was a
transmission job on a 1991 Nissan pickup.
On that unit, the torque converter turbine had lost its teeth and loaded
the transmission cooler with enough metal particles to fill a small pepper
shaker. Removing the radiator, I let the
parts washer run solvent through the trans cooler all night long pumping into
an overflowing drain pan and got a large amount of metal out of it. In spite of the all night flush and the in-line
filter we installed in the return line, the students wound up having to remove
and clean the valve body about six or eight times before the valves ever
stopped sticking. It was astonishing how
those tiny particles of metal can make it past that inline transmission filter
and find their way past the pan filter into the valve body, but it doggone sure
happens!
When the metal comes from somewhere
besides the torque converter, it’s a good idea to flush the converter as well
(if you have the equipment) or replace it, because getting all the metal
flotsam out of the converter is nearly impossible.
In cases like that (to include our
Dakota), it’s wise to either replace the radiator, or if cost is an issue, take
the contaminated cooler out of the loop and install a good quality external
trans cooler. In an attempt to contain
the cost of this job, it was my decision to take a chance on having the
students flush the transmission cooler and lines with denatured alcohol and
trans fluid and install an inline filter in the cooler return line near the
radiator. The inline filter is actually
an authorized repair on Ford vehicles.
The transmission guy at the Ford place rebuilt a
transmission on a 1994 F250 4WD that was going through all its shifts too
soon. His rebuild made no change in the
concern. Wondering if the PCM was at
fault, he called me into the situation and I found a bad 4WD LOW indicator bulb
in the cluster. The PCM looks at voltage
coming through the 4WD LOW indicator light to determine if the transfer case is
in low range. With the transfer case switch grounded, the light illuminates and
kills the voltage, alerting the PCM that low range has been engaged. With no
voltage coming through the bulb, the PCM assumed the transfer case was in low
and altered its shift strategy accordingly.
Back On the Road… Briefly
On re-installation, there was a
problem with the replacement torque converter… Three of the flywheel bolt holes
would line up but the fourth one was about a half-a-hole off, no matter which
way the converter was turned or which holes were used for which bosses. I called the vendor, and he knew right away
what the problem was. He had sent us the
wrong converter, and when he sent the right one, it fit like a charm. It was astonishing that a wrong converter
could be so nearly the same as the right one.
Another guy from an independent shop brought a
1987 Jeep Cherokee around to my service bay at the Jeep dealer saying that he had rebuilt the AW4
transmission because it had to be manually shifted.I fished the transmission computer harness out
from under the passenger sided of the dash and showed him a blown inline
fuse.With a dead TCM, the Jeep takes
off in whatever gear you select with the lever but wont’ shift on its own.Newer Jeeps have that fuse in the PowerDistributionCenter under the hood.
Josh figured he had done a good job
flushing the transmission cooler, so he chose not to install the inline filter
on the return line. As his instructor, I let him make the decision figuring he
would either be lucky as all get-out or he’d learn a hard lesson. After all, that fine paper filter Chrysler has
used for so many years might just do the job.
Test driving the Dodge, revealed a
smoothly operating transmission, but the 3.9L engine had a seriously annoying
misfire under load that made it feel like there were machine guns mounted on
the fenders. I secured the customer’s
approval and we went after the skip.
We found worn plugs and plug wire
boot leaking spark, so I ordered a set of plugs and a single lead from Sam’s
Auto Parts, only to find that it only partially corrected the concern. Another leaking spark plug wire goaded us
into replacing the whole set of wires, which initially seemed to make a big
difference in the performance of the truck, but then the skip returned but with
different qualities. Not only would the
engine misfire under load, but it would misfire intermittently at idle. Nothing
was evident on the o-scope to indicate the cause of the intermittent idle
misfire. This was getting personal, and in the interest of putting the Dakota
back in the wind, I wasn’t about to take it lying down.
In chasing this anomaly, I rapidly
drew a number of conclusions.
A.
The #2 cylinder was the guilty party; it was the one that made no
difference when the spark was shorted away and the skip was present.
B. Allowing the spark to jump to
the plug, I noticed that spark was always popping, even when the misfire was
under way.
C. The injector on cylinder #2 was
clicking away, even during the misfire.
D. The Dakota was outfitted with a
returnless fuel system.
E.
The fuel gauge showed less than an eighth of a tank of gas, but it was
above empty.
Drawing on past experience, I
remembered a late ‘90’s Dodge Van I had encountered a few year earlier with
basically the same fuel system and the same concern. Having been slapped around royally by the van
[we always benefit from those experiences], I took notice of the fact that the
#2 injector was at the highest point on the fuel rail on that side of the
engine; any air bubbles that entered the rail from a cavitating or air-sucking
fuel pump would tend to gather at the mouth of the #2 injector, much the way
aerated fluid gathers at the center of a torque converter. The cheapest and smartest thing to do was add
a couple gallons of gas, which we did.
That fixed the skip (as I figured it would). Another test drive was in order.
Cat’s On the Roof
Josh came
back from his test drive with a long face.
The transmission was hung in high gear.
I smiled inwardly. The inline
filter would have been a good idea. However,
when he re-pulled the pan, we found all three filter screws loose. Somebody had finger-tightened the filter
screws and both students thought the other student had torqued them. Lesson learned, but that wasn’t the worst of
it. In the pan, we found more metal
filings and tiny needle bearings from the overdrive piston thrust bearing.
To make a
long story short, when Josh disassembled the transmission the second time, he
found that he had mistakenly installed the thrust bearing backwards, and the
paper-thin super-brittle races had shattered, allowing the whole bearing to
cross up and come apart.
It just so
happened that I had an electronic version of the same tranny on hand (a junked
42RE that was donation from the Chrysler dealer).
The 42RE doesn’t have a governor, but we were
able to rob an overdrive piston, its thrust bearing, and the accompanying
sliding hub for damage control. The
overdrive clutches are retained with a thin wire retainer rather than a snap
ring, and there was some confusion that resulted from that, but after several
valve body cleanings, everything turned out okay in the end.